Volador VX3.5 Build flight test w/1404 Motors,Caddx Walnut
Автор: B2FPV
Загружено: 2023-08-22
Просмотров: 13782
Test flight beginning:
6:20 Analog sub250g flight with no action camera
11:45 Test flight with Caddx Walnut
Update: I found the culprit for the spinning anomalies: when i was first setting up the flight controller,5.5% minimum throttle seemed to spin the props really agressively compared to my old build so i set it to 3%. this caused the propellers to stall on zero throttle in counterwind and air mode tried to correct this but didn't have enough time to spin up the propellers,but still sent the signal resulting in the rest of the props spinning up and spinning the whole drone into crash. i set it back to 6 percent minimum throttle and tried to cause the same incident on porpuse but couldn't even push the drone out of stability. Now it flies like a dream.
Testing my new build,still have some problems where i suddenly start spinning sometimes when i go upside down,but i'm confident it's just a gyro/accelerometer problem and i can sort it out in betaflight.Other than the problems that are irrelevant to the build,it flies amazing.
Caddx Walnut
4K60 16:9 1/120 ISO100 ND16
FlyFishRC Volador VX3.5 O3 Frame
SpeedyBee F405 Mini 35A BLS
Happymodel 1404 3500KV
Emax Avan 3528 Props
TheFPV Chaos Mini 600mw VTX
Namimno ELRS Flash Nano RX
ORT D-Pole 2.4Ghz
RushFPV Cherry 5.8Ghz
Coddar 650Mah 4S 120c LiHv / Gaoneng 650Mah 4S 120c LiHv
Radiomaster TX12 Mk2
Namimno ELRS OLED TX Module
ORT D-Pole 2.4Ghz
Skyzone SKY04L V2
ORT Helical 3 Turn 5.8Ghz
ORT 6 Leaf Omni 5.8Ghz
Vegas 18 Pro
Cameras used for the off-board footage:
Sony ZV-1
DJI Osmo Pocket
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